Test Firing Day 2 
Sunday, May 31, 2009, 09:24 PM
The team was in a great mood this morning after our successful test firing last night. We started the day with another data and video review of the test firing and an inspection of the rocket motor and test stand in the daylight (was in great shape).

Since we had plenty of time before the planned 2pm public test firing, we took the opportunity to have a morning test firing using our alternative concrete nozzle. This nozzle was manufactured by the team as a backup to our prime graphite/steel composite nozzle. The concrete nozzle was cast using a mold created from the graphite nozzle, high strength concrete, an acrylic binder, and plenty of steel reinforcement.

The test firing was performed without complication, and the motor ran for a planned 5 seconds, reaching 2000 pounds of thrust:



The concrete nozzle performed very well during the test firing. The throat diameter increased ~ XXX% during the burn, and the supersonic section of the nozzle sustained some erosion, but in general the nozzle performed well during the burn. This type of nozzle is an adequate backup for ASA’s activities. Here is a before and after image of the concrete nozzle:



Later in the day, we prepared for our last test firing of the day. We loaded the LOX tank to the 50% position using the liquid level monitoring system, loaded the rest of the alcohol (~XX gallons) and would have been ready for our 2pm test firing….had the LOX tank helium regulator not leaked. When pressurized, the regulator would not control to the set pressure – it kept rising (much faster than LOX boiloff would have caused). After the LOX tank was depressurized, our “red team” (Rob and Michael) went out to the test stand and repaired the regulator (needed a new teflon seal).

20 minutes later, the regulator was repaired and we were ready for the test firing. After a short address to the crowd we counted down to our best test firing to date: a 15 second burn at 2250 pounds of thrust. The ISP is estimated to be ~210 seconds:




In this image, you can see the glass from the ablative liner that was deposited on the supersonic section of the nozzle. This picture was taken after the 15 second burn:



This was a very successful test firing weekend. We had our typical hardware and software troubles but the team worked through them with ingenuity and patience.

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Test Firing Day 1 
Saturday, May 30, 2009, 09:49 PM
After a long day of plumbing and computer troubles, we ended the day with a 2 second test firing of the rocket motor - reaching 1700 lbs of thrust!

We began the day with several water flow tests to measure the alcohol system pressure drop with the new high pressure helium valve. The new data matched the predictions well and provided a reasonable estimate for the LOX side pressure drop with the new helium valve without performing a water test on that system.

After the water flow test, we performed a cold flow test of the new LOX plumbing and level monitoring system: Using liquid nitrogen to simulate liquid oxygen we loaded the LOX tank half full (identified using the new liquid level monitoring system) and let the system sit for ~30 minutes to allow ice to form. Good results all around – no ice on the foam and no ice downstream of the main LOX valve. At this point, we performed a complete hot fire simulation using the liquid nitrogen in the LOX system and water in the fuel system, demonstrating the correct operation of the rocket motor and computer control system. During this test, we observed nitrogen leaking past the main LOX valve. This leak was unacceptable and we spent the next two hours diagnosing and repairing the valve (needed a new teflon shim seal).

After a few more hours of working through issues like the leaky valve, we filled the alcohol tank to the top and the LOX tank to the 25% fill mark (using the new level monitoring system). At last we were ready to test fire the motor. The first countdown occurred around 8:30 pm … but the countdown aborted due to lack of prime ignition! We spent the next ~ 30 minutes pouring through the test data but could not determine why ignition did not occur. Hence, we pressurized the system and tried the countdown again.

This time ignition occurred at the correct time during the countdown. The motor ran for two seconds before the liquid oxygen ran out, reaching ~1700 pounds of thrust:



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Fourth Work Day 
Saturday, May 2, 2009, 08:06 PM
The propulsion team started the day by epoxying the thermocouple patch heaters around the six LOX tank level sensing thermocouples. After a couple of rounds of testing, urethane foam was applied to the tank over the sensors.

Later in the day, the team installed the hopeful fix for our ignitor problems – a pre-mixer for the propane and compressed air. This pre-mixer is located just upstream of the existing ignitor in the port previously occupied by a chamber pressure sensor and thermocouple. The benefit of the pre-mixer was immediately obvious – smooth runs of the ignitor over a much wider range of mixture ratios. With this success, the chamber pressure and ignitor temperature sensors were relocated and the ignition system work was postponed until further combustion testing could be performed in a better location.

In addition to this fix to the ignition system, two backup ignition methods have been identified and will be ready on test day in case they are needed: paper soaked in alcohol placed inside the combustion chamber to burn with the ignition system, and a remotely-ignited road flare to replace the ignition system.

The computer team performed several complete checks of the new software and rewired sensors today, a great milestone for their hard work.

We ended the day with several countdowns and aborts of the integrated propulsion/computer control system. We’re in good shape for the upcoming test firings!

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